Finding a leak that doesn’t exist, and a broken timepiece.

I’ve been having a hard time finding a few problematic issues with the Renault lately. Particularly it had started to leak power steering fluid quite badly, which would mark the floor where parked up and also get onto the auxiliary belt and make that slip.
Looking down from above, past the alternator and air conditioning compressor the pump looked rather wet, so I splashed out $14 and bought a full seal set for the pump. I decided to clean everything up with degreaser and refill the system, to hopefully see where the oil was leaking from.

dismantle

Begin by taking everything out, including battery, battery tray, moving the air conditioner comressor, remove the alternator and the brackets holding it all in.

empty

That leaves good access to the power steering pump. The corrugated plastic tube is the wiring for the front of the car, the braided hose is the gravity feed to the pump from the reservoir.

scrubbed up

Cleaned up the pump with an old toothbrush and engine degreaser. Rinsed it all down with warm water from the potato pump.

clean

Got a bit carried away as I had water left, so I cleaned down the inside of the hood where the oil had flicked off the belt, and the surrounding areas also. Topped up the oil and left it to dry overnight an in the sunshine.

full

Left it for two days, then checked on the level. Unfortunately the oil was all there still.

still oil

Another two days. Nope, there’s still all the oil left in there. The leak has miraculously fixed itself. Normally, hot, cold.. didn’t matter. It would leak regardless of it it was run or not. Now it’s not leaking!

clean pump

The pump is clean and dry, no signs of leakage.

oily frame

The only other place I can see is the return line, from the rack back up to the reservoir. If that has a crack or a pinhole it could be leaking. The engine cradle frame is a bit oily down under the back but I cannot see anything else that would be causing a leak. Further investigation to follow.

The second thing that irked me was the previously well-working clock had quit.

broken display

The display had taken to showing mostly nonsense, or nothing at all.

clock out

Took the dash to bits (again) and liberated the clock from the little cubbyhole it’s attached to.

polished

Cleaned up the smoked plastic section of the clock as it was all scratched and hazy.

components

Figured there were a couple pieces that might have failed and caused it to not work. Replaced the electrolytic capacitor and transistor. No joy.

circuit diagram

Followed the traces and built a diagram of what went where, to get a bit of an idea of how it all worked.

dead

Tested it but the chip was dead. No oscillator, just noise. The clock circuit boards are available, but they are a Jeep Wagoneer part, and as such suffer heavily from Jeep Tax and are therefore expensive.

zeroes

Upside-down image but poking power to the grid brought some nonsense up on the display so the VFD was all still good.

9

Poking about a bit more showed that some of the logic was alive, as various numbers could be liberated. Nothing sensible though.

led

Purchased a little LED clock with voltage and temperature capability for ten bucks, with the intention of fitting it into the clock as shown- looks OK but a little out of place and the very-bright display has no dimming capability.

dismantle

Decided to strip the board down and re-use the VFD, with the new clock module providing the logic. I’ve ordered a little 50V boost converter to drive the VFD, that will be proven to work first then I shall go ahead and get some high voltage transistors, pull the LED’s off the clock and use the output (multiplexed in the same way thankfully) to drive the VFD. Original clock, original display, just now with time, temperature and voltage display. Watch this space for updates.

Boosted.

The past week has been particularly clement in terms of weather- dry, sunny, cool. Unfortunately I have had a bad cold and had been stuck inside.

My brake booster did arrive though.

box

Today, I was feeling much better so decided to tackle fitting it.

clear a space

First thing to do, remove the master cylinder and move all the wires and pipes out of the way.

nut

Most of the nuts holding the booster on were fairly accessible behind the pedals.

ratchet

Deep socket, extension bar and fine angle ratchet made short(ish) work of it, lain upside down in the footwell.

clean

Took the old one out. Surprisingly clean under there.

old booster

The old servo liberated. $10 core return, $12 to ship. I think not.

new booster

Stuck the new one in the hole and bolted it in. Much label.

tidy

Tidied up the pipes and wires better.

done

Boshed it all back together. Had a fairly decent pedal despite having not bled the system up. Brakes now work. I’ll bleed the system up with the MityVac and go from there. Next up, power steering pump seals.

Pipe failure

I had noticed I was slowly losing coolant, and had attributed it to slight leakage at the head gasket but after running the engine up to very warm, the heater return line showed up something interesting. It began to bubble.

stained pipe

Decided to replace this piece of shaped molded pipe. Typically, the side easiest to get to came off, but the difficult to reach part had to be removed forcefully.
knife

Coolant still looks good though (it started out life yellow).

draining

I think it’s an interesting manufacturing flaw, there are 2 similar pinholes along the length of the pipe.

pinhole

Managed to find a roughly equivalent piece at the store.

replacement pipe

Got it all fitted up and bled.

new pipe in place

No more leaks!

radiator

…or are there? Radiator was a bit damp. Thankfully that is from where I’d opened the bleed screw on top of the radiator and it had percolated down the fins inside and come to the surface there.

Redux of the last few months.

It’s been a slow few months with little to report. I’ve lost faith in a few things, with a couple problems and issues with projects that had me baffled and I kinda lost interest in them.

However, things have picked up a little and I’ve gone back to the troubled projects or made some headway.

I bought some replacement tuning slugs for the Marantz receiver. They aren’t 100% the same permeability but they are the correct screw thread.

slugs

Replaced them in the transformer after carefully breaking the old ones up and getting them out of the core. Now I know what they feel like, the old ones were broken before I even started- the lack of decent radio reception certainly points to that.

radio waves

I got all set up and the thing refused to tune well. I could get a couple of strong local stations but the tuning meter and tune indicator would not light up, and those are partially controlled by the transformer. I connected my oscilloscope to the input side of the transformer to check the waveform was not distorted and all of a sudden, LOUD radio, strong signal! Uh.. yeah ok. Reflowed the solder, no effect.. touched the oscilloscope probe to the transformer again gently, and bingo. Strong signal. Touched my finger to it.. improvement. Okay, so it’s a capacitance issue. Experimented and ended up with a 10pF ceramic cap across the terminals to bolster the transformer. Now the selectivity and sensitivity are great. It’s right now the best radio I have in the house for FM stereo.

Carried on with it but now it keeps tripping out into protect. I’ve troubleshot the protect circuit, one of the other boards must have a leaky cap on it somewhere. I need to pull the boards power supplies off one by one and see what fixes it.

Next up, refinished the floors at the house. Edging strip all done in the kitchen:

kitchen skirting board

Finished up in the utility room, flooring strip and the paneling done:

utility room door

Finished up the cabinet around the water heater:

water heater

Pulled the stove to bits and thoroughly cleaned it, the glass particularly was vile.

stove

Finished the floor edge strip in the living room, split the flooring between the two rooms where it was buckling and added a divider to allow for expansion.

living room floor

Rented a floor sanding machine and sanded the floors back, as previously they had looked OK, but having painted the walls and tidied up they were the least well-finished parts of the room.

floor sander

Solid cypress flooring. Smelled real nice when lain bare.

floor stripped

A few coats of polyurethane clear varnish later:

shiny

Looking much better. Also, picked up a nice Holophane light fitting on clearance for $4 at Home Depot. Fitted an LED light to it that has 4 segments inside, looks rather like a standard light bulb:

light fitting

Been troubleshooting the brakes on the car for a while. Stumbled across a post on a Ford Explorer forum with the same symptoms as mine. Turned out to be a faulty brake booster servo. I’m going to vacuum test mine this afternoon, have my MityVac for the purpose (shown here with brake bleeding catch-can fitted):

MityVac

Also picked up a GTE Palco payphone, which has gone into service here at the house, with the requirement for coin removed.

GTE Palco payphone

I repaired a little Realistic PA amplifier that got struck by lightning, and built a cardboard speaker to test it with.

amp and speaker

Also cleaned out and got fixed up the Kerosene lantern, for hurricane use.

kero lantern

That’s about it for now.

Another stereo.

Recently was offered this hi-fi by a work colleague. Garage clear-out, it had been sat in there for years.

Marantz MR1155

It’s a Marantz MR1155, from the early malaise years of cost-cutting and design setbacks. It also didn’t work. Power was applied before I got it, and apparently it went click and made a bit of a crackle.
Sure enough, it would power up and come out of protect, but not much else happened. Evidently the protect circuit was not detecting a particular problem so that was kinda okayish.

dust werewolves

With the lid removed, the contents of the device appeared to be mostly lint. Yuk. That has to be the worst hifi I’ve owned yet in terms of dirt.

clean

Thankfully it all cleaned up nicely.

stripped down faceplate

Pulled the front off after work, removed all the buttons (they had gone green and fusty) and brought it all home to clean up. Judicious application of drill and polishing mop got it looking respectable again.

shiny

Not perfect by any means but definitely better.

lid

Cleaned up and put the lid back on. Fairly respectable.

in bits again

Brought it all home and started to poke about. Pulled up the manual off HifiEngine and set about looking for the cause of no audio. Powered it up, the main amp voltages were pretty much in spec, but the FM/AM/Phono/Preamp board was dead, with hardly any voltage. Bypassed the preamp board and fed the power amp board directly- presto, greeted with slightly clipped but definitely OK audio. The expensive amplifier modules are still OK.

caps

Ordered the full replacement of electrolytic caps to shotgun all the boards. Over the course of a couple days I replaced everything. Still no voltages, so I replaced the transistors that control the voltage and protect circuit.. nothing much. Further troubleshooting found the 14V Zener to be almost a dead short over 0.3V so I went to desolder it and it cracked into 2 pieces. With it removed, bringing up the variac got the voltages to rise. There’s the problem then. Ordered a couple 14V Zeners and whilst in town stopped at Radio Shack and picked up a couple 12V ones to see if that would get it to come to life:

alive!

Sure enough. Not very good but operational. Went to tune the FM because it was not working very well at all post e-cap replacement. Broke the discriminator tuning slug (even using a fiberglass tool of the correct size) so pulled that out and took it to bits. Ordered a couple replacement cores, so need to wait until it’s all back together before readjusting.

10.7MHz transformer

Go figure. It had to break..

Reflective! Also, frosty.

Bought a mirror from a gentleman in Canada.

mirror

Bottom one (old) being held up. Sunshine and humidity made all the silver fall off. The new one looks new by comparison.

Also moved the car and mowed because the grass is growing fast this season.

grass

That’s 4 days’ worth of grass growing around here.

frozen

Also the new heater element arrived for the freezer. Not a day too soon, it was beginning to freeze up. That again was 4 days’ of ice.

Brake bias valve

I finally decided to disregard the service manual and remove the brake safety/bias valve assembly as bleeding the brakes resulted in the pedal becoming solid halfway down its travel and not really doing much. Bought an open ended ring spanner (flare nut wrench) and some PlusGas releasing agent. Sprayed it all up and let it sit before attacking it with the wrench.

wrench

After a while it was all undone.

valve gone

Offending item out. It’s not very big, but it’s milled from a chunk of aluminum.

grubby

Looking into it showed that it was kinda grubby. Undid the safety shuttle valve assembly.

end cap

Yeah, that’s meant to be very clean inside there. It wasn’t.

shuttle valve

The shuttle valve end. It was firmly stuck in position, that’ll be why the brakes didn’t want to bleed properly, then.

piston

Had to hammer it out. It was covered in crusty, solidified old brake fluid. Cleaned it up. Surprisingly the seals are still good.

shuttle done

With the shuttle valve cleaned out, I undid the bias valve assemblies, which were similarly dirty but at least not stuck (too much) and cleaned them out.

all clean

Reassembled it all and put it back in the car. I now need to bleed the system. Hopefully now it’ll be good.

Speaker grille redux

Finally, I added another coat of stain to the grille face of the speaker that I rebuilt.

drying grille

Sat on the cardboard box in the back of the truck to dry in the sunshine. Plank of plywood next to it for the PSU project I’ve been building.

Once the stain had soaked in it got buffed off and left in the sun a while, then I gave it a coat of Tung oil and let that set.

cloth

Measured and cut the cloth. Stretched and stapled it into place on the spacers.

fixed grille

Added the badge back on and put it in place. Looks sharp!

Multi-cap can

Had a bit of spare time and inclination today so I took all the connections off the back of the McIntosh after labeling the wires. That’s a task in itself.
Removed the old multi-cap can. Took to the base of it with the Dremel. I had wanted to retain the original look of the capacitor as the top of it sticks through the chassis. The old brown heat marks show the point where it shows. The Dremel cut is well below the visible line.

dermelled

Mallory’s finest. Still in surprisingly good physical shape.

can dissected

Cleaned the dregs of tar out of the case after softening it a bit in boiling water.

tarpit

Removed the old capacitor wad. Four new caps to fit inside. It would appear Nichicon listened to the classic audio crowd because these are common values and voltages the the era, designed to fit inside old cans easily.

new bits

Fitted the caps all in place. They fit nicely. Actually over the spec of the originals on voltage and temperature. They should last.

newcaps

Had to drill the base to pull the leads through. Kept the original markings intact.

square triangle semicircle

Glued back together it looks nice. Gave it a bit of a buff up with a bit of metal polish.

restuffed

Looks neat back in the chassis. Sitting listening to it now and it’s running happily.

Much more brakes

grunge

Mmmmm.

Weather today was nice enough and I had the day off so I set up on the ramps and pulled my brakes to bits.

pot of gold

Old stuff to come out wasn’t horrible but I’ve certainly seen better.

master cylinder

New master cylinder.

clean fluid

New fluid. Certainly better than the old. Tried vacuum bleeding the system but ended up with an infinite supply of bubbles and not much fluid so called SWMBO in to shove on the pedal a bit.

Net result is brakes, but I did notice that the back section of the reservoir would never empty when bleeding, only the front. Pedal is better and the brakes are fairly sharp but now it feels like you hit the sliding shuttle inside the master cylinder and it’ll go no further. I think the bias valve is stuck one way and only working the system on half of the, er, system. The other half of the system then just making pressure against the valve and it going nowhere.

I’ll have to get a split-O 12mm to try and get that undone- 6 pipes that have never been undone that are steel into aluminium. That bodes.

I might try and source a replacement first.. not sure if it’s a Bendix part or Renault or none of the above.

Square one. I hate brakes.